Please use this identifier to cite or link to this item: https://repository.sustech.edu/handle/123456789/19846
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dc.contributor.authorAhmed, Abdullah Ahmed Jibreel-
dc.contributor.authorMustafa, Abduallah Hashim MohaemdElahassan-
dc.contributor.authorAbdallah, Jafar Mohamed Jafar-
dc.contributor.authorSupervisor-, WidaatallahAlamin-
dc.date.accessioned2018-01-08T07:32:21Z-
dc.date.available2018-01-08T07:32:21Z-
dc.date.issued2017-10-01-
dc.identifier.citationAhmed, Abdullah Ahmed Jibreel.Lean Six Sigma for Productivity Improvements/Abdullah Ahmed Jibreel Ahmed,Abduallah Hashim MohaemdElahassan Mustafa,Jafar Mohamed Jafar Abdallah;WidaatallahAlamin.-Khartoum : Sudan University of Science and Technology, College of Engineering,2017.-61 p. :ill;28cm.- Bachelors search.en_US
dc.identifier.urihttp://repository.sustech.edu/handle/123456789/19846-
dc.descriptionBachelors searchen_US
dc.description.abstractThe main goal of the project is the Implementation of lean Six sigma which is a methodology aim to improve the productivity by systematically removing of waste, reduce defects and variation. The methodology is divided into five steps “Define, Measure, Analyze, Improve and Control (DMAIC)”. This case study was carried at engineering company in cutting tools section on specific product “Cone Drill”. The five steps of DMAIC methodology was implemented on the product to reduce the total manufacturing time and reduce the variation which contribute in improving the productivity and decrease the total manufacturing time and cost, also give a less amount of waste. In define phase data have been collected problems and objectives, measured. Data analyzed using MiniTab and Excel and detected the root causes of the problems. By brainstorming best solution carried out. Problems solved and made improvements on total manufacturing time. In control phase improvements monitored and controlled by using check process form. The final results was the total manufacturing time decreased from 130.95 minutes to 70 minutes and this decreased the total cost of the Milling, Lathing, and Sharpening processes cost from 72.6 SDG to 41.3 SDG per unit which this decreased the cost by 43% from previous cost.en_US
dc.description.sponsorshipSudan University of Science and Technologyen_US
dc.language.isoenen_US
dc.publisherSudan University of Science and Technologyen_US
dc.subjectProductivity Improvementsen_US
dc.subjectLean Six Sigma for Productivity Improvementsen_US
dc.titleLean Six Sigma for Productivity Improvementsen_US
dc.typeThesisen_US
Appears in Collections:Bachelor of Engineering

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